2 Votes (3.50 Moyenne) et 1.448 Vues  

Cessna 206 Stationair (N3800G) - Aircraft crashed in 2004. Photo taken in 1993 during a Florida trip: The airline transport certificated pilot was flying passengers and a cameraman associated with a film production to film a fort on an island. During the filming, the pilot stated he switched fuel tanks, and noted that the left tank was full, and the right tank about 3/4 full. As the airplane approached the fort, the engine sputtered, and then regained full power. A minute or two later, the pilot indicated the engine lost all power, and after unsuccessfully trying to restart it, he ditched the airplane. The pilot and passengers were all able to exit the airplane except the cameraman, who tied himself to the seat with a rope prior to takeoff after the cargo door had been removed to facilitate filming. Attempts to free the cameraman prior to the airplane sinking were unsuccessful, and he drowned. A passenger noted that the right fuel tank fuel gauge was somewhere around the 1/4 mark, and bouncing as the airplane flew. Postaccident inspection of the airplane, recovered 17 days later from ocean waters, disclosed no evidence of any pre-impact mechanical malfunction. CAUSE: A loss of engine power for an undetermined reason during cruise flight, which resulted in the pilot ditching the airplane in ocean waters.
/images/icons/csMagGlass.png moyen / grand / plein format

Cessna 206 Stationair (N3800G)

Soumis

Aircraft crashed in 2004. Photo taken in 1993 during a Florida trip: The airline transport certificated pilot was flying passengers and a cameraman associated with a film production to film a fort on an island. During the filming, the pilot stated he switched fuel tanks, and noted that the left tank was full, and the right tank about 3/4 full. As the airplane approached the fort, the engine sputtered, and then regained full power. A minute or two later, the pilot indicated the engine lost all power, and after unsuccessfully trying to restart it, he ditched the airplane. The pilot and passengers were all able to exit the airplane except the cameraman, who tied himself to the seat with a rope prior to takeoff after the cargo door had been removed to facilitate filming. Attempts to free the cameraman prior to the airplane sinking were unsuccessful, and he drowned. A passenger noted that the right fuel tank fuel gauge was somewhere around the 1/4 mark, and bouncing as the airplane flew. Postaccident inspection of the airplane, recovered 17 days later from ocean waters, disclosed no evidence of any pre-impact mechanical malfunction. CAUSE: A loss of engine power for an undetermined reason during cruise flight, which resulted in the pilot ditching the airplane in ocean waters.

Comments

Please log in or register to post a comment.

JOURNAL DE L'ACTIVITE
Vous voulez une recherche complète sur l'historique de N3800G depuis 1998? Achetez maintenant. Recevez-le dans l'heure.
Date Avion Provenance Destination Départ Arrivée Durée
No Recent History Data
Les utilisateurs élémentaires (l'inscription est gratuite et facile !) peuvent voir 3 months d'historique. S'inscrire
 

Se connecter

Vous n'avez pas de compte? Inscrivez-vous maintenant (gratuitement) pour des fonctionnalités personnalisées, des alertes de vols, et plus encore!
Saviez-vous que le suivi des vols FlightAware est soutenu par la publicité ?
Vous pouvez nous aider à garder FlightAware gratuit en autorisant les annonces de FlightAware.com. Nous travaillons dur pour que notre publicité reste pertinente et discrète afin de créer une expérience formidable. Il est facile et rapide de mettre les annonces en liste blanche sur FlightAware ou d’examiner nos comptes premium.
Abandonner